Hexapod
From Experimental Robotics
Work Required
- At least one of the servo motors has burnt out. It will need to be replaced.
- The current battery needs to be replaced with a lower voltage one (hence problem above).
See Also
- http://www.lynxmotion.com/ - the platform
- http://www.newmicros.com/ - ServoPod to control servo motors
- http://www.sparkfun.com/ - BlueSMiRF RS232 wireless serial link
